I'm experiencing high CHT's and EGT's during climb-out, which I have not noticed before. Two days ago I did a test-flight to record engine data on my GRT Horizon HS, and was able to open the files and read it last night. I am looking for suggestions as to the cause of the high temps.
Here's the test-flight data, all at mixture full/in, OAT 34F.
After takeoff, at 1,000' ASL just before pulling back on throttle and RPM, I have CHT's (F) (#1,2,3,4) 451, 413, 453, 423, and EGT's 1490, 1572, 1486, and 1479.
FF was max 15.9 gph, with an average of around 14.5 during the climb.
At 1,000', at 24 squared, temps settled in at 423, 407, 422, 387, and EGT's 1407, 1445, 1397, 1403
with FF 8.1
At 1,000', at 20 squared, temps settled in at 369, 376, 178*, 338, and EGT's 1338, 1372, 1317, 1306,
with FF 6.8
Some other data:
RV-7a, approx 750 TT eng and airframe.
O-360-A1A, c.s prop.
Carburetor was originally Marvel Schebler MA4-5 10-4164-1, which was replaced approx 300 hrs ago with a 10-3878, with no discernable difference in temps.
Mag timing has been checked, both withing +/- 1 degree.
Mixture cable has been checked, its correct, with carb's micture level against it's stop when mixture control full forward.
I've checked for induction leaks, around induction tubes and carb/sump gasket, but haven't found any.
Any suggestions on what the root cause might be? What to do next, how to fix it?
Thanks!
Here's the test-flight data, all at mixture full/in, OAT 34F.
After takeoff, at 1,000' ASL just before pulling back on throttle and RPM, I have CHT's (F) (#1,2,3,4) 451, 413, 453, 423, and EGT's 1490, 1572, 1486, and 1479.
FF was max 15.9 gph, with an average of around 14.5 during the climb.
At 1,000', at 24 squared, temps settled in at 423, 407, 422, 387, and EGT's 1407, 1445, 1397, 1403
with FF 8.1
At 1,000', at 20 squared, temps settled in at 369, 376, 178*, 338, and EGT's 1338, 1372, 1317, 1306,
with FF 6.8
Some other data:
RV-7a, approx 750 TT eng and airframe.
O-360-A1A, c.s prop.
Carburetor was originally Marvel Schebler MA4-5 10-4164-1, which was replaced approx 300 hrs ago with a 10-3878, with no discernable difference in temps.
Mag timing has been checked, both withing +/- 1 degree.
Mixture cable has been checked, its correct, with carb's micture level against it's stop when mixture control full forward.
I've checked for induction leaks, around induction tubes and carb/sump gasket, but haven't found any.
Any suggestions on what the root cause might be? What to do next, how to fix it?
Thanks!
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