Today while shooting a practice approach, I felt a consistent engine miss when descending and the throttle pulled back. I quickly looked at the engine monitor and #1 and #2 EGTs had fallen way off compared to the other two cylinders. Adding some power cleared it up, pulling the power started the missing. The next flight I did a really thorough run up and all looked good. The flight home didn't see the problem .
I might have pushed the mixture in much higher than normal!! My safety pilot said he heard some popping but it didn't catch my attention
Here's the engine data graph.
IO-360-M1B
1 mag, 1 P-Mag
Any thoughts?
I might have pushed the mixture in much higher than normal!! My safety pilot said he heard some popping but it didn't catch my attention
Here's the engine data graph.
IO-360-M1B
1 mag, 1 P-Mag
Any thoughts?