This engine was assembled new in Jan 2011. It was flown 114hrs between new and the end of 2021 when I purchased the plane from the builder. Since then it has flown another 110 hrs until the present by me. The engine has performed flawlessly during my ownership. (Hot) compressions on 4-17-25 were #1 78 #2 74 #3 78 #4 80 all over 80. The past 3 annuals the compressions have all been in the mid 70s cold.
Here's a link to the boroscope taken on the 4-17th. This is the first boroscope I have done on the engine. Considering the fact that it has performed flawlessly and the compressions have been consistently good, I was a little alarmed with these photos. If anyone sees red flags here, please point them out. The lineup of the photos are jpg 001-009 #1, 010-019 #3 020-029 #4 030-043 #2. I'd really appreciate your opinion/analysis of what you see. . Here's a link to the boroscope results.
drive.google.com
Here's a link to the boroscope taken on the 4-17th. This is the first boroscope I have done on the engine. Considering the fact that it has performed flawlessly and the compressions have been consistently good, I was a little alarmed with these photos. If anyone sees red flags here, please point them out. The lineup of the photos are jpg 001-009 #1, 010-019 #3 020-029 #4 030-043 #2. I'd really appreciate your opinion/analysis of what you see. . Here's a link to the boroscope results.
988GH Boroscope 4-17-25 - Google Drive
drive.google.com