dick seiders
Well Known Member
First flight scheduled SAturday last did not occur as ignition check at 4000rpm showed a significant drop on the B side. A side was 115 drop, B was 460 or so. Switched module wiring around all possible ways today with no change in B performance. All indications point to stator/trigger coil problems based on input I rec'd from Dean at Lockwood. (Larry's suggestion, thanks, Larry). Has anyone else experienced this difficulty, and if so what were the remedies? I have also been advised by Rotax owners to make certain the carbs are in sync before pulling the engine. This of course makes sense if indeed that is a possible contributor, but I am not confident about that as a solution. I would of course be estatic if it was. Not looking fwd to yanking a brand new engine out out of my 12. Any input greatly appreciated.
Dick Seiders
Dick Seiders