I’ve recently started flying my Rocket With its updated G3X panel and auto pilot servos. The roll servo tuning went pretty well and performs well. Pitch servo works terrible. I’ve followed the tuning guide sent to me by Garmin support but no amount of adjustment helps. The basic issue is the pitch control is
vague and imprecise. Like the system is constantly chasing itself. Raising gain/lowering gain has the expected results but the response is still vague. It’s as if the pitch servo were connected with rubber bands. Elevator control system is butter smooth with the auto pilot off. The elevator returns to its neutral position when displaced. One thing I noticed is that with the AP on there is a fair amount of free play in the servo before you feel the torque resisting movement of the stick. Is this normal? My old Tru Trak system (which flew perfectly) did not have this free play.
vague and imprecise. Like the system is constantly chasing itself. Raising gain/lowering gain has the expected results but the response is still vague. It’s as if the pitch servo were connected with rubber bands. Elevator control system is butter smooth with the auto pilot off. The elevator returns to its neutral position when displaced. One thing I noticed is that with the AP on there is a fair amount of free play in the servo before you feel the torque resisting movement of the stick. Is this normal? My old Tru Trak system (which flew perfectly) did not have this free play.
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