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05-01-2018, 06:19 PM
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Join Date: Oct 2007
Location: Salmon Arm, BC
Posts: 933
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Fuel Pressure loss on Loop upline
Airplane - F1 Rocket, IO-540 D4A5, recent install of Red Cube between fuel servo and spider. Engine driven fuel pump has ~350 hours.
Pulling 3 g's at the start of a loop I am experiencing a fuel pressure loss from the normal 20+ psi to ~8 psi (engine loses power) after which my boost pump automatically kicks in (power picks back up) and brings the pressure back to normal.
I can fly around all day, pulling 2 g's in 60* banks, and no issues, fuel pressure stays 20+ psi.
Anybody experience the same? Am I correct to assume a new engine driven fuel pump is in my near future?
__________________
Mark Olson
1987 RV-4 Sold
2003 Super Decathlon - Sold
F1 EVO Rocket, first flight May 31/14
First in line for the Sonex JSX-2T kit
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05-02-2018, 05:50 AM
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Join Date: Oct 2005
Location: 08A
Posts: 9,476
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Consider the changes you made, and start there.
First, it worked fine prior to relocating the red cube, yes?
I assume you're measuring pressure at the engine pump outlet. If so, nothing you plumbed between the throttle body and the divider would make a difference.
I further assume the red cube was previously firewall mounted between the bulkhead fitting and the engine pump. If so, you changed a hose and/or hard line as part of the relocation.
Thus three possibilities; the new lines pick up more heat than the previous install, or one of the fittings has a small air leak, or you installed a right angle fitting and (combined with heat) it is forming vapor bubbles in the flow.
__________________
Dan Horton
RV-8 SS
Barrett IO-390
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05-02-2018, 07:12 AM
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Join Date: Apr 2010
Location: Ridgeland, SC
Posts: 2,583
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Mark----did you have previous flights in this configuration and 3g's with no issues?
Tom
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Tom Swearengen, TS Flightlines LLC, AS Flightlines
Joint Venture with Aircraft Specialty
Teflon Hose Assemblies for Experimentals
Proud Vendor for RV1, Donator to VAF
RV7 Tail Kit Completed, Fuse started-Pay as I go Plan
Ridgeland, SC
www.tsflightlines.com, www.asflightlines.com
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05-02-2018, 07:27 AM
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Join Date: Aug 2005
Location: Dallas/Ft Worth, TX
Posts: 5,665
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Quote:
Originally Posted by SMO
Pulling 3 g's at the start of a loop I am experiencing a fuel pressure loss from the normal 20+ psi to ~8 psi (engine loses power) after which my boost pump automatically kicks in (power picks back up) and brings the pressure back to normal.
I can fly around all day, pulling 2 g's in 60* banks, and no issues, fuel pressure stays 20+ psi.
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20 PSI "normal" is too low (18 minimum), typical pump pressure should be around 24-26, I'd start there.
__________________
Walt Aronow, DFW, TX (52F)
EXP Aircraft Services LLC
Specializing in RV Condition Inspections, Maintenance, Avionics Upgrades
Dynamic Prop Balancing, Pitot-Static Altmeter/Transponder Certification
FAA Certified Repair Station, AP/IA/FCC GROL, EAA Technical Counselor
Authorized Garmin G3X Dealer/Installer
RV7A built 2004, 1700+ hrs, New Titan IO-370, Bendix Mags
Website: ExpAircraft.com, Email: walt@expaircraft.com, Cell: 972-746-5154
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05-02-2018, 05:00 PM
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Join Date: Oct 2007
Location: Salmon Arm, BC
Posts: 933
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Quote:
Originally Posted by DanH
Consider the changes you made, and start there.
First, it worked fine prior to relocating the red cube, yes?
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I have had 10 flights since the change where I performed some aerobatics, only the last 3 - 4 have shown these symptoms. BTW, the other change I made at the same time was replacing my Andair gascolator with and Aerolab.
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I assume you're measuring pressure at the engine pump outlet.
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Correct, just to clarify this is not a measurement issue, there is a corresponding loss of engine power till the boost pump cuts in.
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I further assume the red cube was previously firewall mounted between the bulkhead fitting and the engine pump.
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Close, it was a Floscan that was replaced, and it was located in the tunnel between the stick well and the firewall. Replacement hose is a straight run.
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Thus three possibilities; the new lines pick up more heat than the previous install, or one of the fittings has a small air leak, or you installed a right angle fitting and (combined with heat) it is forming vapor bubbles in the flow.
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To add the Red Cube I put a bracket on the front of the fuel servo and mounted the cube there. Not a likely source for additional heat.
Will check the fittings for a leak, although why "G" forces would exacerbate a leak I am not sure, but possible.
No right angle fittings were introduced.
EDIT: This is not fuel flow related, I have confirmed via flight testing.
__________________
Mark Olson
1987 RV-4 Sold
2003 Super Decathlon - Sold
F1 EVO Rocket, first flight May 31/14
First in line for the Sonex JSX-2T kit
Last edited by SMO : 05-03-2018 at 09:42 PM.
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05-02-2018, 05:05 PM
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Join Date: Oct 2007
Location: Salmon Arm, BC
Posts: 933
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Quote:
Originally Posted by Walt
20 PSI "normal" is too low (18 minimum), typical pump pressure should be around 24-26
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I should have been more clear, the normal fuel pressure fluctuates between ~22 and ~25. If I look at this on a graph it has a very constant oscillation - is that oscillation normal?
__________________
Mark Olson
1987 RV-4 Sold
2003 Super Decathlon - Sold
F1 EVO Rocket, first flight May 31/14
First in line for the Sonex JSX-2T kit
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05-02-2018, 08:31 PM
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Join Date: Sep 2005
Location: Maple Grove, MN
Posts: 2,329
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Quote:
Originally Posted by SMO
I should have been more clear, the normal fuel pressure fluctuates between ~22 and ~25. If I look at this on a graph it has a very constant oscillation - is that oscillation normal?
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Approximately what is the frequency? I've noticed this at about 2400 RPM as monitored by the G3x Touch. I believe it may have to do with the sampling frequency of the engine monitor vs pressure pulses in the mechanical pump. Unverified, but the oscillation goes away when I dial the rpm down from 2400 to about 2350. The period of the osc. I have observed is about 5 seconds, and it will vary between maybe 21 and 25.
__________________
Alex Peterson
RV6A N66AP 1700+ hours
KADC, Wadena, MN
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05-02-2018, 09:33 PM
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Join Date: Oct 2005
Location: 08A
Posts: 9,476
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Quote:
Originally Posted by SMO
I have had 10 flights since the change where I performed some aerobatics, only the last 3 - 4 have shown these symptoms. BTW, the other change I made at the same time was replacing my Andair gascolator with and Aerolab.
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So check it for an air leak. Seal the inlet and pull suction on the outlet, see if it will hold a vacuum.
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Will check the fittings for a leak, although why "G" forces would exacerbate a leak I am not sure, but possible.
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If fuel weighs 3x more, it requires 3x the pressure drop for the same lift. More suck means a small air leak becomes a big air leak. Entrained air doesn't pump very well.
Hey, it's the long distance diagnosis game, with the usual lack of information. Maybe right, maybe not, but I usually have a logical reason for a suggestion.
__________________
Dan Horton
RV-8 SS
Barrett IO-390
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05-02-2018, 09:50 PM
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Join Date: Nov 2010
Location: ____
Posts: 829
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location, location, location
Where did you mount the aerolab relative to the exhaust tips?
Or how many inches aft of the firewall? I am guessing it is somewhere in the center tunnel belly skin.
I am also guessing on take off, below 500ft, you have your boost pump on?
The exhaust pulse is a vibrational shake and bake to anything on the floor skin near the center tunnel. Might just be bubbles manifesting from the increased flow demand when you pull the nose vertical. A 2 G level turn will need less power and fuel flow than a 3 or 3.5 G pull up.
Last edited by F1R : 05-02-2018 at 10:20 PM.
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05-02-2018, 10:42 PM
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Join Date: Oct 2007
Location: Salmon Arm, BC
Posts: 933
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Quote:
Originally Posted by DanH
So check it for an air leak. Seal the inlet and pull suction on the outlet, see if it will hold a vacuum.
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This I will do
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..... but I usually have a logical reason for a suggestion.
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Of that I have no doubt.
__________________
Mark Olson
1987 RV-4 Sold
2003 Super Decathlon - Sold
F1 EVO Rocket, first flight May 31/14
First in line for the Sonex JSX-2T kit
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