|
-
POSTING RULES

-
Donate yearly (please).
-
Advertise in here!
-
Today's Posts
|
Insert Pics
|

09-28-2013, 09:59 PM
|
|
|
|
Join Date: Nov 2011
Location: Alameda CA
Posts: 4
|
|
Mysterious Ailment
The right O-320 of a GA-7 Cougar has developed a sudden high mag drop in both mags, as much as 160RPM. Observation 1: leaning the mixture decreases the drop to about 120. Observation 2: leaning the mixture on the left engine has a negligible affect on its normal drop of about 50-60RPM each mag.
The left mag acted normal during one brief runup session, but now produces similar RPM loss as the right as when the problem first surfaced. The right mag seems to be more seriously affected than the left, so our diagnostic efforts thus far have addressed the right mag. Diagnostic 1: swapped plugs top to bottom to switch the plugs driven by each mag. No effect. Diagnostic 2: swapped the right mag from the left engine. No effect. Mag timing to engine is correct.
A hot compression check yielded 74, 70, 72 & 72. Plugs are clean and dry top & bottom, no oil fouling of any kind. The high mag drop is accompanied by a very mild roughness. Running on both the engine develops smooth power equal to the left engine (no yaw trim req'd during flight).
We're out of ideas - any imaginative thoughts here?
Thanks!
|

09-28-2013, 10:15 PM
|
 |
|
|
Join Date: Aug 2005
Location: Dallas/Ft Worth, TX
Posts: 5,668
|
|
Running overly rich will cause a high mag drop on both mags.
__________________
Walt Aronow, DFW, TX (52F)
EXP Aircraft Services LLC
Specializing in RV Condition Inspections, Maintenance, Avionics Upgrades
Dynamic Prop Balancing, Pitot-Static Altmeter/Transponder Certification
FAA Certified Repair Station, AP/IA/FCC GROL, EAA Technical Counselor
Authorized Garmin G3X Dealer/Installer
RV7A built 2004, 1700+ hrs, New Titan IO-370, Bendix Mags
Website: ExpAircraft.com, Email: walt@expaircraft.com, Cell: 972-746-5154
|

09-28-2013, 10:55 PM
|
 |
|
|
Join Date: Jan 2005
Location: 57AZ - NW Tucson area
Posts: 10,011
|
|
Quote:
Originally Posted by airportkid
....A hot compression check yielded 74, 70, 72 & 72. ...
|
If those numbers were using a "Bonanza" compression checker with a 0.060 orifice instead of the Lycoming recommended 0.040 orifice, then you could have low compressions.
Some mechanics just use the one they have without checking the orifice size... 
__________________
Gil Alexander
EAA Technical Counselor, Airframe Mechanic
Half completed RV-10 QB purchased
RV-6A N61GX - finally flying
Grumman Tiger N12GA - flying
La Cholla Airpark (57AZ) Tucson AZ
|

09-28-2013, 11:13 PM
|
 |
|
|
Join Date: Jun 2006
Location: 8I3
Posts: 3,562
|
|
I would have swapped the plugs between engines first.
__________________
Please don't PM me! Email only!
Bob Japundza CFI A&PIA
N9187P PA-24-260B Comanche, flying
N678X F1 Rocket, under const.
N244BJ RV-6 "victim of SNF tornado" 1200+ hrs, rebuilding
N8155F C150 flying
N7925P PA-24-250 Comanche, restoring
Not a thing I own is stock.
|

09-29-2013, 09:03 AM
|
|
|
|
Join Date: Jan 2005
Posts: 1,024
|
|
Make sure the carb heat door isn't leaking hot air into the airbox. and also make sure the primer isn't leaking extra fuel into the intake system.
Good Luck,
Mahlon
__________________
"The opinions and information provided in this and all of my posts are hopefully helpful to you. Please use the information provided responsibly and at your own risk."
|

09-29-2013, 10:24 AM
|
|
|
|
Join Date: Apr 2010
Location: Ridgeland, SC
Posts: 2,584
|
|
Glad to see Mahlon on the forum!!!!!!
Hi Mahlon!
Tom
__________________
Tom Swearengen, TS Flightlines LLC, AS Flightlines
Joint Venture with Aircraft Specialty
Teflon Hose Assemblies for Experimentals
Proud Vendor for RV1, Donator to VAF
RV7 Tail Kit Completed, Fuse started-Pay as I go Plan
Ridgeland, SC
www.tsflightlines.com, www.asflightlines.com
|

10-01-2013, 09:35 PM
|
|
|
|
Join Date: Nov 2011
Location: Alameda CA
Posts: 4
|
|
Quote:
Originally Posted by mahlon_r
... Make sure the carb heat door isn't leaking hot air into the airbox. and also make sure the primer isn't leaking extra fuel into the intake system ...
|
Now why didn't we think of that! We'll check the carb heat door straightaway and post the result. Too much of my recent life spent fixing injected engines - I forgot all the gadgets on the carbureted ones. Thanks!
|

10-03-2013, 12:50 PM
|
 |
|
|
Join Date: Oct 2011
Location: Atlanta
Posts: 875
|
|
Also
Swap the left and right engines, retest.
Sorry, couldn't resist 
__________________
RV-8 IO-360 (Bought)
RV-6 O-360 C/S (Sold)
Walkman aka Flame Out
|

10-03-2013, 06:03 PM
|
|
|
|
Join Date: Nov 2011
Location: Alameda CA
Posts: 4
|
|
Quote:
Originally Posted by airportkid
... We'll check the carb heat door straightaway and post the result ...
|
Well, it's not that. We've now completely transposed the right mag ignition system engine to engine, plugs, harness and mag, with no effect - the right mag on the right engine loses 160-170RPM and is subtly rough, even though every component of it has been taken from the left engine. Meanwhile, of course, the removed system installed on the left engine operates perfectly.
Could carbon buildup on the piston or elsewhere in the head degrade the force of the mixture charge when fired from one source? The plug appearance is normal in all cylinders, showing no signs of detonation.
Still haven't tried inverting half the harness to fire all the top or bottom plugs from one mag, but would that tell us anything?
|

10-03-2013, 06:32 PM
|
 |
|
|
Join Date: Dec 2008
Location: Ontario, Canada
Posts: 464
|
|
Next time you run the engine, laser temp the cylinders to make sure they are all around the same temp( no cool cylinders). Check for intake leaks at same time.
|
Posting Rules
|
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts
HTML code is Off
|
|
|
All times are GMT -6. The time now is 09:30 PM.
|