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  #11  
Old 04-27-2015, 03:32 PM
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My thought is that the fuel servo interprets a lower pressure within the body (relative to the external static pressure) with higher velocity airflow through the device so will add fuel. Correct?
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  #12  
Old 04-27-2015, 06:06 PM
Rupester Rupester is offline
 
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The FI regulator (aka servo) measures intake air velocity and increases fuel flow accordingly. i.e. more power demand increases measured intake air velocity and resultant fuel dispensed by the regulator. If the intake were blocked, I would think the regulator would see very low intake velocity and hence flow reduced fuel. I must be missing something here.
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  #13  
Old 04-27-2015, 07:22 PM
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Quote:
Originally Posted by Jesse View Post
First of all, at that power setting, 11gph seems way too low, ....
My fuel flow instrumentation (GRT) has proved to be accurate in the past. At 23 squared I can normally pull the FF down under 10 gph before it stumbles - injectors are balanced so peak egt happens on each cylinder within ~.2 gph.

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Originally Posted by Jesse View Post
Since it is a rocket, it makes me wonder if it was the flight attitude that caused the low reading.
Attitude was straight and level flight.

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Originally Posted by BillL View Post
Well - I am not sure if you are saying this was sucked in the air intake, or was sucked into the alt air door from the lower cowl.
I believe the plastic bag was blocking the air intake and the alt air door operated as it should, sucking in hot air from the lower cowl.

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Originally Posted by DanH View Post
That's a phenomenon Don measured on the AFP flow bench. This spring loaded alternate air door caused a fuel flow increase with the primary intake blocked, although not nearly as much as the 9 GPH in your graph.
I have a Precision Silverhawk RSA-5 fuel servo, not sure if that makes any difference. There is undoubtedly differences in the spring tension and the alternate air door size and shape. Also, would Don's measurements change based on parameters for an IO-540 (assuming his measured increase was based on a 4 cylinder)?

At the end of the day I cannot state for certain what caused this, but given its isolated nature (two more normal flights today) and the presence of the bag beside the airplane after it was shut down, its the only thing that makes sense to me. However it may have been something else and the presence of the bag was a coincidence. I may never know unless it happens again.
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  #14  
Old 04-27-2015, 08:40 PM
molson309 molson309 is offline
 
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I had the Vans original alternate air door on my RV-7A. It was held closed by a magnet. I found out that under cruise or higher power it would open due to the pressure difference across the air filter and I got results as you describe - a very high fuel flow. I could cause it to happen by a slight change in throttle position and it baffled me until I realized that the door was opening when it should not have. This airplane used Airflow FI, but I can imagine Bendix would probably give the same results - the disturbed airflow through the servo caused mismetering of fuel. A spring loaded one could very well cause the same problems.

Removing that door and going to the sliding one Vans now sells completely cured the problem.
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  #15  
Old 04-28-2015, 06:05 AM
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Quote:
Originally Posted by SMO View Post
I believe the plastic bag was blocking the air intake and the alt air door operated as it should, sucking in hot air from the lower cowl.
That's why I did mine as a spring loaded door rather than a manual control; no pilot action required to continue flight. And I think your bag theory is a good one. You could check it easy enough; do a quick runup on the ramp, record the MP, RPM and fuel flow, then shove the bag into the intake and do it again.

Quote:
I have a Precision Silverhawk RSA-5 fuel servo, not sure if that makes any difference.
The Silverhawk does sense pressure differently, using a low-gain venturi rather than the high gain venturi of the FM series fuel controls.

Quote:
There is undoubtedly differences in the spring tension and the alternate air door size and shape.
I sized the spring so the door starts to open at around 3" H2O pressure differential across the filter element (actually designed for 2", but it turned out to be 3" on the flow bench). The arm to which the spring is attached has less and less advantage as the door opens, so the force necessary to open the door does not rise much as it opens further. The long spring helps too; less tension rise with length increase. I think arranging the leverage to offset rising spring pressure is a key point to the design of a spring loaded alternate air door.





Quote:
Also, would Don's measurements change based on parameters for an IO-540 (assuming his measured increase was based on a 4 cylinder)?
The difference would merely be increased air flow demand. If all airbox dimensions were proportionally larger to match, the numbers would probably be the same

Break.

I looked up the measured numbers for the above airbox. At 1400 lbs per hr air flow, carb loss was 3.1" H2O for a bare FM200 with an inlet bell, 5.0" with the filtered airbox, and 6.2" with the airbox inlet completely blocked and the alternate air door floating open in equilibrium with air pressure. Fuel flows were 122 lbs per hr, 123 lbs per hr, and 130 lbs per hr respectively. You're reading that correctly; blocked inlet and alternate air door operation only increased fuel flow about 5%.
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  #16  
Old 04-28-2015, 06:11 AM
Robert Anglin Robert Anglin is offline
 
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Location: houston, texas
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Default You win!

Looks good that you had the alt. air door to catch your chocked intake. Brings back old engine stories when we would put our hand over the intake and turn it over a few times to chock it before start up. Only one tip out of this old f_ _ _. You may wish to clean your spark-plugs a little early as a heavy chock or rich event will tend to dirty them up a lot faster. Thanks for post, I think I will go pull the air filter off the mower and not us the chock to start it, just hand-cup the intake and pull it through a couple of times. It is good to stay in practice. Yours as always. R.E.A. III #80888
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  #17  
Old 04-28-2015, 06:23 AM
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Quote:
Originally Posted by Rupester View Post
The FI regulator (aka servo) measures intake air velocity and increases fuel flow accordingly. i.e. more power demand increases measured intake air velocity and resultant fuel dispensed by the regulator. If the intake were blocked, I would think the regulator would see very low intake velocity and hence flow reduced fuel. I must be missing something here.
One side of the air diaphragm is ported to dynamic pressure (the 4 little tubes in the throat of a Bendix or Silverhawk) and the other side is ported to venturi pressure. The higher the differential, the more the diaphragm moves against a fixed spring, further opening the fuel control ball valve. If I have my theory correct, a blocked filter increases fuel flow due to the increased drop at the venturi (suction, if you prefer) while dynamic pressure remains roughly the same, a function of RPM.
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  #18  
Old 04-28-2015, 08:06 AM
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vlittle vlittle is offline
 
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Quote:
Originally Posted by DanH View Post
That's a phenomenon Don measured on the AFP flow bench. This spring loaded alternate air door caused a fuel flow increase with the primary intake blocked, although not nearly as much as the 9 GPH in your graph.

Dan, where did you get your cowl scoop/air box set up? It looks like such a thing could be adapted to my smooth Hr-ii cowl that has the inlet just below the spinner.
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  #19  
Old 04-28-2015, 08:35 AM
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Quote:
Originally Posted by vlittle View Post
Dan, where did you get your cowl scoop/air box set up? It looks like such a thing could be adapted to my smooth Hr-ii cowl that has the inlet just below the spinner.
It's all scratch-built, processes detailed in the fiberglass section of the forums.
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