Quote:
Originally Posted by gereed75
I had this problem also due to poor workmanship when drilling the hole in the weldment that holds the tailwheel spring. My drilled hole on the bottom of the weldment had some slop and allowed the tailwheel spring to rotate in the socket - my fix:
I had a local machine shop turn a conical washer from 4130 high strength steel. The washer was about .4" thick and the ID bore was a tight fit on the AN 4 bolt. The shoulder of the washer was turned into a cone shape with a 100 degree angle (the same as the angle under the head of a countersink AN screw). I then used a 100 degree countersink as a cutter and cut the 100 degree countersink through the weldment and into the tailspring. The bolt (a slightly longer one than stock, to provide room for the conical washer and to keep the washer on the bolt shoulder) was installed and tightened, and the conical washer was pulled into the countersunk surface (sort of like a valve seating in an angled valve seat).
This whole thing can be done from a 3/4" access hole drilled into the fuse bottom, just below the spring retainer bolt.
I believe that this is a good fix because it actually increases the surface area of contact between all the mechanisms involved. It also pulls the tailspring weldment into tension against this 100 degree seat, while taking out all play. Also you now have some compression holding the assembly together and you are just not relying on the shear of the bolt against the tailwheel weldment to counteract the twist forces of the spring in the weldment.
So far so good. 40+ hours, a few not so pretty landings and my spring remains secure.
If there is judged to be merit in this fix, and interest, I will try to post the sketch I made of the conical washer and the whole fix as it looks assembled.
A peer review discussion is welcome.
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Your description was perfect. I can not comment on the integrity of your fix as I dont know how much side loading there is on the tail wheel that produces the torque on the spring. I suspect your fix is better than the original "hole through the tube" though.
Mine was a QB fuselage and I suspect the factory did not do a good job when drilling those holes. Interestingly enough, my 3 kit has the tailwheel assembly all drilled and bolted together as it came. It is tight, tight, tight.
I will keep your fix in mind if mine should worsen on my 6.
Good thing is, both parts are steel and nothing critical is going to happen even if it is a bit loose. Just something to watch over time. Worse case over time, I could change out the weldment, a bit tight in there, but doable. I would try your fix before I went that far. Thanks.