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  #11  
Old 02-09-2009, 10:46 PM
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JonJay JonJay is offline
 
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Default Fixed, but not with JB weld.

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Originally Posted by JonJay View Post
I am going the JB Weld route as recommended by a couple AP's. I will let you know how it works out.
Further investigation yielded little hope for the JB weld. The spring to socket tolerance is just too tight. My issue is a rotation, where the spring turns or rotates in the socket, not a loose spring itself.
I was able to press in Close Tolerance Bolts for the two An3's in the tail wheel socket and that took all of the slop away there. A close tolerance 174 in the fuselage took away much of that play as well, but there is still a small amount. I am going to live with it and hopefully it will not work the hole anymore.
There was a thread on here some time ago about a home plating kit. An idea might be to plate an AN4 and build it up beyond what a Close Tolerance bolt is.
Moving on now. Good luck with yours Steve.
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  #12  
Old 02-10-2009, 09:01 AM
gereed75 gereed75 is offline
 
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I had this problem also due to poor workmanship when drilling the hole in the weldment that holds the tailwheel spring. My drilled hole on the bottom of the weldment had some slop and allowed the tailwheel spring to rotate in the socket - my fix:

I had a local machine shop turn a conical washer from 4130 high strength steel. The washer was about .4" thick and the ID bore was a tight fit on the AN 4 bolt. The shoulder of the washer was turned into a cone shape with a 100 degree angle (the same as the angle under the head of a countersink AN screw). I then used a 100 degree countersink as a cutter and cut the 100 degree countersink through the weldment and into the tailspring. The bolt (a slightly longer one than stock, to provide room for the conical washer and to keep the washer on the bolt shoulder) was installed and tightened, and the conical washer was pulled into the countersunk surface (sort of like a valve seating in an angled valve seat).

This whole thing can be done from a 3/4" access hole drilled into the fuse bottom, just below the spring retainer bolt.

I believe that this is a good fix because it actually increases the surface area of contact between all the mechanisms involved. It also pulls the tailspring weldment into tension against this 100 degree seat, while taking out all play. Also you now have some compression holding the assembly together and you are just not relying on the shear of the bolt against the tailwheel weldment to counteract the twist forces of the spring in the weldment.

So far so good. 40+ hours, a few not so pretty landings and my spring remains secure.

If there is judged to be merit in this fix, and interest, I will try to post the sketch I made of the conical washer and the whole fix as it looks assembled.

A peer review discussion is welcome.

Last edited by gereed75 : 02-10-2009 at 09:04 AM.
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  #13  
Old 02-10-2009, 09:18 AM
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JonJay JonJay is offline
 
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Default Sounds like a decent solution.

Quote:
Originally Posted by gereed75 View Post
I had this problem also due to poor workmanship when drilling the hole in the weldment that holds the tailwheel spring. My drilled hole on the bottom of the weldment had some slop and allowed the tailwheel spring to rotate in the socket - my fix:

I had a local machine shop turn a conical washer from 4130 high strength steel. The washer was about .4" thick and the ID bore was a tight fit on the AN 4 bolt. The shoulder of the washer was turned into a cone shape with a 100 degree angle (the same as the angle under the head of a countersink AN screw). I then used a 100 degree countersink as a cutter and cut the 100 degree countersink through the weldment and into the tailspring. The bolt (a slightly longer one than stock, to provide room for the conical washer and to keep the washer on the bolt shoulder) was installed and tightened, and the conical washer was pulled into the countersunk surface (sort of like a valve seating in an angled valve seat).

This whole thing can be done from a 3/4" access hole drilled into the fuse bottom, just below the spring retainer bolt.

I believe that this is a good fix because it actually increases the surface area of contact between all the mechanisms involved. It also pulls the tailspring weldment into tension against this 100 degree seat, while taking out all play. Also you now have some compression holding the assembly together and you are just not relying on the shear of the bolt against the tailwheel weldment to counteract the twist forces of the spring in the weldment.

So far so good. 40+ hours, a few not so pretty landings and my spring remains secure.

If there is judged to be merit in this fix, and interest, I will try to post the sketch I made of the conical washer and the whole fix as it looks assembled.

A peer review discussion is welcome.
Your description was perfect. I can not comment on the integrity of your fix as I dont know how much side loading there is on the tail wheel that produces the torque on the spring. I suspect your fix is better than the original "hole through the tube" though.
Mine was a QB fuselage and I suspect the factory did not do a good job when drilling those holes. Interestingly enough, my 3 kit has the tailwheel assembly all drilled and bolted together as it came. It is tight, tight, tight.
I will keep your fix in mind if mine should worsen on my 6.
Good thing is, both parts are steel and nothing critical is going to happen even if it is a bit loose. Just something to watch over time. Worse case over time, I could change out the weldment, a bit tight in there, but doable. I would try your fix before I went that far. Thanks.
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  #14  
Old 02-10-2009, 11:07 AM
gereed75 gereed75 is offline
 
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I also looked at removing the weldment - and I also judged it doable but lots of work. If my fix doesnt hold up long term, that is what I will do. But so far so good. I think the fix is pretty robust.

If a new weldment became necessary, I think I would also consider beefing up the wall thickness of the weldment in this location with a doubler welded on to give it all a bit more beef.

Hope it never comes to that.

Fly on. Be safe.
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