|
-
POSTING RULES

-
Donate yearly (please).
-
Advertise in here!
-
Today's Posts
|
Insert Pics
|

03-27-2018, 02:10 PM
|
|
|
|
Join Date: Sep 2006
Location: Windsor, California
Posts: 920
|
|
In addition to the RotaxOwner videos, there are a couple of videos on YouTube that depict the servicing of Bing carbs -- not necessarily by the book but they do have some good visuals of the carb's internals.
__________________
David Heal - Windsor, CA (near Santa Rosa)
EAA #23982 (circa 1965) - EAA Technical Counselor and Flight Advisor; CFI - A&I
RV-12 E-LSA #120496 (SV w/ AP and ADS-B 2020) - N124DH flying since March 2014 - 940+ hours (as of September 2020)! 
V AF donation through June 2021.
|

03-27-2018, 02:23 PM
|
 |
|
|
Join Date: Oct 2005
Location: 08A
Posts: 9,476
|
|
Quote:
Originally Posted by DaleB
Is there a compelling reason to ship them off to let someone else overhaul, or is this a no-brainer for guys who have some clue which end of the screwdriver is pointy?
|
No-brainer.
CV Bings are very simple, and have not really changed in 40 years.
Worst case, you throw them in a box later and ship them to a shop.
FYI...We lost a 2 stroke Kitfox here some years ago and traced the fuel stoppage to a small piece of trash hidden in the carb's fuel inlet nipple, i.e just upstream of the the float valve. Nobody ever looks there.
__________________
Dan Horton
RV-8 SS
Barrett IO-390
Last edited by DanH : 03-27-2018 at 02:25 PM.
|

04-21-2018, 06:26 AM
|
|
|
|
Join Date: Jan 2005
Location: Kentucky Lakes area in KY
Posts: 947
|
|
Quote:
Originally Posted by bob1393
Thanks Scott and others for the reply. We have the new floats and did check them at 200 hours and they were fine. We did not check them again at 400 hours. We will check them now and the gascolator also to see if there is any debris or contamination as well as weigh the floats.
Bob
|
Hey Bob, Were you successful in solving your carb problem? I have the same problem and I am currently working on it........Tom
__________________
2013- RV12, Kit #119. N123M First flight Nov21. It's a keeper!
1998- RV-9 tail kit, built and sold
1989- RV-6 tail kit, built and sold
|

04-21-2018, 03:39 PM
|
 |
|
|
Join Date: Apr 2007
Location: Madison, AL
Posts: 338
|
|
I ran into the same issue in December and did an engine shut down and power off landing. Went through many carb clean/flush with no debris evident. Ended up draining all auto gas and switch to 100LL with fuel system flush. No problem since. Was thinking old ethanol gas had some fuel line deposits.
__________________
Scott- 2020 donation
New RV-7A N579RV, only 80 hours now without 2020 fly-in destinations
Built RV-12, 328 hours-sold, purchased RV-12 sold, Built RV-9A, 536 hours-sold, Not completed RV-7 sold, Built Kitfox sold
|

04-21-2018, 09:36 PM
|
|
|
|
Join Date: Jun 2014
Location: Port Orchard, Wa
Posts: 84
|
|
Todehnal - next morning it started and ran perfectly. We did swap out the Ducati Voltage Regulator. We've been flying it and have not had any issues. I'm thinking dirt or debris in fuel line someplace or in the carb that has worked itself through. We're coming up soon on the 500 hour inspection and we'll see what we find. Let me know if you uncover anything.
Bob
|

04-22-2018, 01:00 PM
|
|
|
|
Join Date: Jan 2005
Location: Kentucky Lakes area in KY
Posts: 947
|
|
Hey Bob, glad yours is running well. I'm still in trouble here. I replaced the plugs, pulled the float bowls and inspected. I did adjust the fuel level slightly. Those were the easy things. Next, I plan to pull the carbs and do a tear down inspection. From the replies that I've received, most suggest that the likely suspect is a carb problem. It is hard to diagnose. You would think that a shut down and inspection of the plugs after a rough run situation would point you to the problem. Apparently that is not the case with Rotax. I understand that the rough running shakes the **** out of the carbs, the floats go nuts and flood everything. In my case, all four plugs in cylinders #1 and #2 were totally sooted up, as was the tail pipe. I will post any finds...........Tom
__________________
2013- RV12, Kit #119. N123M First flight Nov21. It's a keeper!
1998- RV-9 tail kit, built and sold
1989- RV-6 tail kit, built and sold
|

04-22-2018, 01:50 PM
|
|
|
|
Join Date: Sep 2006
Location: Windsor, California
Posts: 920
|
|
Also check for debris in the return fuel line metering orifice.
__________________
David Heal - Windsor, CA (near Santa Rosa)
EAA #23982 (circa 1965) - EAA Technical Counselor and Flight Advisor; CFI - A&I
RV-12 E-LSA #120496 (SV w/ AP and ADS-B 2020) - N124DH flying since March 2014 - 940+ hours (as of September 2020)! 
V AF donation through June 2021.
|

04-22-2018, 03:40 PM
|
|
|
|
Join Date: Jan 2005
Location: Kentucky Lakes area in KY
Posts: 947
|
|
Quote:
Originally Posted by DHeal
Also check for debris in the return fuel line metering orifice.
|
Now that does surprise me that this could cause a rough engine, but it is an easy check. Thanks.....Tom
__________________
2013- RV12, Kit #119. N123M First flight Nov21. It's a keeper!
1998- RV-9 tail kit, built and sold
1989- RV-6 tail kit, built and sold
|

05-05-2018, 08:03 PM
|
 |
|
|
Join Date: Sep 2017
Location: Gig Harbor
Posts: 36
|
|
Its all better now.
This is Art, one of Bob's partners. The problem with our rough running engine was some contamination in one of the carb float bowls. We think the contaminant was from chaffing of one of the floats. Keith (one of the three owners) found a small initially hard object. After extracting it from the float chamber he was able to crush it between his fingers. We think it would intermittently clog the jet causing the engine roughness. We have flown several hours since without any problems. Also, Lockwood in FL was very helpful in steering Keith in the right direction.
|
| Thread Tools |
Search this Thread |
|
|
|
| Display Modes |
Linear Mode
|
Posting Rules
|
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts
HTML code is Off
|
|
|
All times are GMT -6. The time now is 05:23 PM.
|