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  #1  
Old 11-26-2016, 07:33 PM
Aero_Octaveus Aero_Octaveus is offline
 
Join Date: Aug 2014
Location: Edmonton, AB
Posts: 216
Default This sting of poor rivets

Well, I have gone and done it. Totally ruined my left aileron trying to rivet the skin to the main spar. What an awful area to try and rivet. The spar flange has a slight acute angle to it which presents a bit if a challenge to get the bucking bar at an angle to help sit flush with the rivets. I used just about every method I could think of to try and rivet these properly. I used a small oak shim in an attempt to prop up, or adjust the tungsten bucking bar to the appropriate angle. I've tried different bucking bars, different angles, different shims, taking angry, talking pleasant, massaging it, giving it a break, everything!!!! and in the end, every rivet shop head wants to dump to the same side every time. Of course once a dimpled rivet hole has been dumped now the nightmare begins. Will it dump again, well chances of it going awry are growing. Too many times, now an opps rivet. ****! the oops rivet has dumped...They all dump in the same direction. After about 3 hours if consistently terrible rivets all dumped the same direction I have successfully ruined a potentially perfect aileron.

Just a sampling of how ALL of the rivets wanted to set...



Today....building my plane has not brought joy to my life!!
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RV-7A - Emp and Wings Done. Working on fuse

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Last edited by Aero_Octaveus : 11-26-2016 at 07:48 PM.
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  #2  
Old 11-26-2016, 07:50 PM
wirejock's Avatar
wirejock wirejock is offline
 
Join Date: Oct 2005
Location: Estes Park, CO
Posts: 3,931
Default Shop heads

Bummer. Sorry you had a bad day.
I would suggest a method ut it sound like you tried them all including the one I used. I used a shimmed tungsten bar. I learned the perfect shim always seems to be more angle than looks right. Practice on that one till you find a method that works for the next one.
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  #3  
Old 11-26-2016, 08:12 PM
gasman gasman is offline
 
Join Date: Mar 2007
Location: Sonoma County
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Default

Is that a shadow (gap) between the parts?
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Old 11-26-2016, 09:00 PM
Aero_Octaveus Aero_Octaveus is offline
 
Join Date: Aug 2014
Location: Edmonton, AB
Posts: 216
Default

Thanks Wirejock. The tough part is I can for the life of me figure out why they were doing this. I'm really worried I will mess it up again if I order another aileron. The right aileron gave a me bit of trouble but it worked out alright. But the left....it was just a runaway train. The angled portion of the bucking bar was perpendicular with the rivet head. Should have set straight. I even tried holding the bar in my fingers without any guide. Same result. Maybe there was some sort of side load on the rivet when setting them. Maybe the three skins/spar where slightly out of alignment.

Looking at my parts graveyard....I think I see enough parts for three planes!
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Old 11-26-2016, 09:07 PM
David Paule David Paule is offline
 
Join Date: Dec 2009
Location: Boulder, CO
Posts: 4,428
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Here's how I solved the problem on my RV-3B ailerons.

On mine, the spar flange to skin was difficult. This C-shaped tool and a handy box end wrench did the job nicely.

Dave
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  #6  
Old 11-26-2016, 09:35 PM
Aero_Octaveus Aero_Octaveus is offline
 
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Location: Edmonton, AB
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Whoa David!!! Million thanks to you!!! You have been there too and solved it. (I see you ruined an aileron too...guess I shouldn't feel too bad as this is a tough one to rivet).

I guess that answers how to avoid screwing up another aileron!
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  #7  
Old 11-26-2016, 09:51 PM
rv7charlie rv7charlie is offline
 
Join Date: May 2006
Location: Pocahontas MS
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Default

No idea if this will work for you; everybody's different. But IIRC, I had more luck in those situations by ignoring the side structure & 'calibrating' my fingertips/thumb tip to feel for the bar's surface being parallel to the flange/skin. I also 'cheat' with neoprene or rubber sheet that's roughly the same thickness (better if slightly thicker) as the unset rivet tail length. A square or disc with a #40 hole drilled in it will hold the rivet in place, help keep the bar parallel to the flange, and help clinch the skin/structure together. Once the rivet is partially set, you can go to a thinner sheet, or trust your calibrated fingertips. :-)

To re-square the dimples, have you used the trick of putting the male die in a rivet set die-holder, and a shop-made female 'die' drilled/countersunk into a bucking bar? Line everything up, and give it a *light* tap or 3 with the gun. Obviously, everything needs to be lined up for this to work.

FWIW,

Charlie
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  #8  
Old 11-27-2016, 08:50 AM
SgtZim SgtZim is offline
 
Join Date: May 2015
Location: Crittenden, ky
Posts: 194
Default

I recall making a lot of rivets like that.

I think what helps me - basics

- make sure the rivets fit the hole well, not loose, and not sticking up on the manufactured head. Only touch up the hole if the rivet won't go into position with a good push. If a rivet feels too loose or too tight in a hole - try another - there are variances in the manufacture of these things.

-if the mfg head is not sitting nicely in the dimple or countersink, touch the dimple up with your countersink bit - very lightly to make it lay in snug.

- use rivet tape even if you don't need it to keep the rivet from falling out

- I like to use LOTS of clecos. Every other hole at least on most parts. Some parts I cleco every hole and only pull the ones where I am riveting.

- I like to start driving with a very short burst to set the rivet snug in the hole, and follow with a longer brrrrt.

- if at all possible, clamp your piece down to keep it from moving too much.


I think these set up items are probably more important than the angle of the bucking bar.
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Last edited by SgtZim : 11-27-2016 at 08:52 AM.
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  #9  
Old 11-27-2016, 09:29 AM
David Paule David Paule is offline
 
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Location: Boulder, CO
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Quote:
Originally Posted by David Paule View Post
Here's how I solved the problem on my RV-3B ailerons.

On mine, the spar flange to skin was difficult. This C-shaped tool and a handy box end wrench did the job nicely.

Dave
Worth mentioning is that I visited my mentor's shop not long ago, considerably after I'd done this, and on a wall he had a number of different-sized C devices like this that he'd made for his project.

Dave
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  #10  
Old 11-27-2016, 03:07 PM
Aero_Octaveus Aero_Octaveus is offline
 
Join Date: Aug 2014
Location: Edmonton, AB
Posts: 216
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Wish we had a Yard Store in Canada. To get a C-Frame Rivet set up here is gonna cost me about $60
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