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Did another SB today. Probably took about 1.5 hours because cowl was already partially off. Very easy project. If anybody wants help, hop over to X35 and we'll help, powder coat and all.
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All done and back flying. Picture as promised!
![]() And yes?..the welded edge did get primed and painted after I took that photo. Clearly not easy to get the paint on from the angle we painted at. All up probably a bit over 30 man hours. And all my EGT/CHT connections are flaky :( so I have to decowl and squeeze the spade sockets for a tighter fit. But otherwise no leaks and flying/taxiing well. One thing I noticed with the new rubbers and thicker plate is the nose is higher and tail lower. By a fair amount too! |
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Vic, did you feel the doubler and the reinforced ring design was going to be better? What did Vans say about that? |
Yes.
Yes, I think the new ring brace will be fine. I had to put the doubler on mine as the hole in the initial plate was too large. The doublers that they are sending out for those who don't have cracks have a larger diameter hole as they don't need to have the close tolerance. Unfortunately, I had already welded it in before it was recognized as the wrong part.
Vic |
SB Completed
Started my nose gear SB last week and could not get the WD-1015 collar assembly off. Tried hard for a couple of days, but it would not budge. Called Jesse Saint over in Dunnellon at X35 and arranged to take the airplane to him this morning. Jesse and his team finally managed to get the collar off. A bit of corrosion on the top of the link assembly was the reason I could not get it off, as we suspected. Anyway, no cracks.
750 hours in 5 1/2 years operated on hard surface most of the time. Most of the grass strips I have landed on have been pretty smooth. The only exception to that is some transition training I did for a couple of pilots that requested grass field work. I used Pierson, FL, 2j8, and Bob Lee Strip, 1j6, near Deland, FL and they were both pretty rough. I have not used them again. I have used the airplane for Transition Training for the past three years, so had some concerns because of the high number of landings. (I have not kept track of the number of landings on the airplane) Happy to report that the nose gear was in great shape. Jesse and I talked about the use of RTV on the doubler, and he, of course, said it was up to me whether to use it or not. He has used it on the other airplanes he has done. I elected to use it. If you are in central FL, stop at X35 and visit Jesse. His operation is impressive. Some of the cheapest 100LL in the area, as well. |
SB Done Yesterday
Inspected my -10 last Friday and found no cracks. Got the part frm Vans Tuesday and went to the airport after work on Wed to verify the fit and paint it. Did some minor cleaning up with a dremmel tool and have a good fit.
Installed it after work last night in about an hour including putting the cowl on etc. Needed only one spacer to preload it so the elastomers have not compressed much. Shaft looks good too with no noticable wear. Total of 500 hours with 99% on paved surfaces. Kit number 40142, built in 2005 (think it was the 13th RV-10 flying). I had replaced the nose gear bushings at around 350 hours but verified they were all ok while I had it apart. As others have said, easy fairly quick job if you have no cracks. Hardest part was getting the collar off.:) TJ |
SB done
SB completed. 480 hours based at grass field. No cracks. SB pretty simple if you have no cracks.
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When I went to inspect my nose gear mount I noted that I did have play in the assembly and that I hadn't checked this in previous condition inspections even though I had removed the wheel each time. I just didn't have it in my checklist. Yes, I think it's important. |
Serial #65 540 Hours no cracks, less than 5 landings on grass.
No wear on any pivot points. Installed one pre load spacer at initial assemble and one additional at about 100 hours. Dick Sipp RV-4 sold, RV-10, RV-12 |
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